Installation
It's called a development/proving model for a reason. Before installation, I did a bench check of the board to test both the EFB bias and screen supply regulator functions of the board to make sure they would both react properly with a changing B+ level applied. The test revealed a small glitch that was basically due to the characteristics of (some of) the newer components I used for the actual build, versus the junk bin parts I used to prove the basic model. A short off course excursion was made to deal with that issue, which has now been put to rest. As a result of this little distraction however, sharp eyes will note a couple of additional components on the board, which now works perfectly.
Planing is everything in a project like this, and it paid off well in this case. The board dropped right into place, and mounted up as planned. One (original) screw mounted the L-bracket, and after a small dab of silicon grease was applied to the Mosfet, a small machine screw, lock washer and nut mounted it down through a screw hole that helps to mount the RF tuner assembly in place. This required the bottom cover of the RF tuner to be removed for access to install the hardware, but otherwise, the mechanical installation was uneventful.
Two groups of 3 wires lead from the board down through two of the cooling holes provided around the tuner filter cap. One group contains the B+ in, EFB screen supply regulator output, and ground leads, while the other contains the two AC power leads from the bias winding of the power transformer, and EFB bias supply regulator output leads. Heat shrink tubing is used to separate these lead groups, and protect them where they pass through the chassis cooling holes to prevent any chafing of the wires. The original bias supply components remain as Avery installed them, with the original white bias supply lead to the output tubes simply disconnected, isolated, and neatly tucked away. The EFB bias supply regulator output lead connects to the point where the original white bias lead was removed from.
Just as the original bias supply lead has been islolated, the screen grids also need to be isolated from their original power supply (but remain connected together), so that they can be powered from the EFB board. This requires removal of the of the original 1.2K 7 watt resistor, and replacing it with a 2.2K 2 watt resistor. Because the screens are now isolated from the original screen supply, this new resistor can be moved over into the power supply area, and connected between the main B+ cap terminal, and original screen grid filter cap terminal. This resistor is raised in value since it no longer has any screen grid current passing through it. Therefore, to maintain the original voltage drop produced by the original resistor, it must be raised slightly now.
All of the connections from the EFB board then either connect to existing connections (i.e, the ground, B+, and AC power leads), or replace an existing connection (the screen power and bias supply leads).
The sum of invasive modifications made to accommodate EFB then includes:
1. Installation of 10 ohm resistors at the cathode of each output tube socket, and
2. Disconnecting and isolating the original bias supply wire from its original connecting point in the output stage area, and
3. Isolating the screen grids from the original screen grid supply, and replacing the original screen grid dropping resistor with a new resistor.
Additionally, a terminal strip was added at the top rear of the chassis, with leads running to the cathode terminals of each output tube. With the EFB bias control accessible from the top side of the chassis now (on the EFB board), and the cathode terminals now accessible top side as well, it makes for very easy bias adjustments on the amplifier. The terminal strip and its leads were also accommodated by small cooling holes at the rear of the chassis, so again, no physical alterations were made for the installation of EFB in the 400.
Side Bar: Many folks prefer to install IBAM circuits, which the EFB modification will easily accommodate. Whether such controls are present or not, I always prefer to install a quad of well matched tubes, as this not only helps ensure the best push-pull balance within a given channel, but also ensures the best performance match between channels as well. My 400 does not currently have an IBAM installed, but does employ a tightly matched quad of NOS tubes, making adjustment of the bias very easy now.
With the EFB modification fully installed now, basic tests were run (on full AC power) to see where things stood. Observations include:
1. Power output remains exactly as it was in stock form, with each channel individually producing 25 watts RMS @ 1 kHz by itself, or 22.5 watts RMS each, with both channels driven.
2. Full power 1 Khz THD with both channels driven now produces an average of just .15% THD. This is a very low distortion level, approaching that of some of the very best vacuum tube amplifiers, and is a major improvement over the original design, where both channels were averaging .95% THD with both channels driven.
Side Bar: Much (>50%) of this is due to the EFB screen supply regulator tightly managing the screen voltage now. In the original design, the screen voltage dropped about 55 volts under worst case conditions, destroying the original low distortion operating point of the stage as power was increased. With EFB, the screen voltage still drops slightly, but now, about 1/5 of the original amount -- and most importantly -- it drops in exact relation to any drop in the plate B+ supply, helping to preserve the low distortion operating point. For pentode output stages, effective control of the screen grid is one of the single most important design requirements to maximize performance from the stage.
3. Because the EFB bias and screen supply regulators both provide significant filtering in addition to providing EFB action, residual power supply hum is now extremely low. Measurements were not made regarding this, but it is now very hard to tell if the unit is even turned on through my Cornwalls with the volume at minimum. Subjectively, there is virtually no power supply hum.
4. Original tests indicated that the low distortion point would be achieved with a total quiescent idle current of 22 ma per tube. But those tests were not actual EFB tests, but simulated EFB tests. With the real deal installed, the low distortion point came in at just 21 ma total quiescent current per tube. This is an unbelievably conservative mode of operation for 7591/7868 class tubes. With an actual plate B+ of 425 vdc, and figuring that 20 ma is flowing to the plate (to account for screen current), that equates to a plate dissipation of just 8.5 watts per tube -- which is just under 45% of the rating for the tube. If that doesn't extend tube life, then nothing will!
5. At quiescent conditions, the screen grids are now running at just over 300 vdc. This is nearly a 100 volt drop from what they were running in the stock design, which has taken away all the stress that the stock design placed on them. The EFB screen supply regulator now maintains the new screen/plate voltage relationship regardless of AC power, power output, or B+ level conditions, maintaining the low distortion operating point of the output stage whether each individually, or both channels are driven to any power level up to maximum power output. An additional huge benefit of the new operating conditions is that the screen grids no longer show any color at all, even when grossly over-driven. This too will have a huge effect not only on tube life, but also in maintaining the tubes' original match conditions: Since the screens now run so much cooler, they will not be inclined to distort their shape, which will help preserve either the original match characteristics of a quad or pair, or the that of the individual tube.
6. The new operating conditions in the output stage not only do not require any screen stability resistors to be installed (although they won't hurt if already installed), but also almost certainly will not require the control grid return resistors to be lowered either. Because the tubes now run so cool (in tube degrees that is), the chance of any reverse grid current effects under the new operating conditions is virtually nil. Like the screen stability resistors, lowering the grid return resistor values certainly won't hurt -- although the phase inverter won't like you for doing it. But that will be dealt with in the next installment.
7. After 3 hours of operation, the power transformer was nicely warm to the touch, but hardly hot, and you could easily keep your entire hand on it for as long as you wished. This is out of case of course, but subjectively, it feels notably cooler than with the stock circuit. With a reduction of quiescent current in the output stage of nearly 45 ma, this equates to over 100 ma of current no longer being drawn from the power transformer, considering its voltage doubler configuration, and the charging current required by the doubler caps for the operating current saved.
Pics include:
1. The completed board awaiting installation, glitch free. Green lead group is for the EFB bias supply regulator, red lead group is for the EFB screen supply regulator.
2. Close up detail of the Mosfet mounting. In operation, there is no discernible heat generated by the Mosfet after hours of normal operation, or 1/2 hour of operation at full power output in both channels, ensuring its long life.
3. Detail of the lead groups dropping below the chassis.
4. The completed top side installation. The bias control is easily accessible at the top right of the board.
5. Terminal strip for monitoring output tube current draw.
Next time: Underside shots of the installation, and clean up work: dealing with that pesky phase inverter.
Dave
It's called a development/proving model for a reason. Before installation, I did a bench check of the board to test both the EFB bias and screen supply regulator functions of the board to make sure they would both react properly with a changing B+ level applied. The test revealed a small glitch that was basically due to the characteristics of (some of) the newer components I used for the actual build, versus the junk bin parts I used to prove the basic model. A short off course excursion was made to deal with that issue, which has now been put to rest. As a result of this little distraction however, sharp eyes will note a couple of additional components on the board, which now works perfectly.
Planing is everything in a project like this, and it paid off well in this case. The board dropped right into place, and mounted up as planned. One (original) screw mounted the L-bracket, and after a small dab of silicon grease was applied to the Mosfet, a small machine screw, lock washer and nut mounted it down through a screw hole that helps to mount the RF tuner assembly in place. This required the bottom cover of the RF tuner to be removed for access to install the hardware, but otherwise, the mechanical installation was uneventful.
Two groups of 3 wires lead from the board down through two of the cooling holes provided around the tuner filter cap. One group contains the B+ in, EFB screen supply regulator output, and ground leads, while the other contains the two AC power leads from the bias winding of the power transformer, and EFB bias supply regulator output leads. Heat shrink tubing is used to separate these lead groups, and protect them where they pass through the chassis cooling holes to prevent any chafing of the wires. The original bias supply components remain as Avery installed them, with the original white bias supply lead to the output tubes simply disconnected, isolated, and neatly tucked away. The EFB bias supply regulator output lead connects to the point where the original white bias lead was removed from.
Just as the original bias supply lead has been islolated, the screen grids also need to be isolated from their original power supply (but remain connected together), so that they can be powered from the EFB board. This requires removal of the of the original 1.2K 7 watt resistor, and replacing it with a 2.2K 2 watt resistor. Because the screens are now isolated from the original screen supply, this new resistor can be moved over into the power supply area, and connected between the main B+ cap terminal, and original screen grid filter cap terminal. This resistor is raised in value since it no longer has any screen grid current passing through it. Therefore, to maintain the original voltage drop produced by the original resistor, it must be raised slightly now.
All of the connections from the EFB board then either connect to existing connections (i.e, the ground, B+, and AC power leads), or replace an existing connection (the screen power and bias supply leads).
The sum of invasive modifications made to accommodate EFB then includes:
1. Installation of 10 ohm resistors at the cathode of each output tube socket, and
2. Disconnecting and isolating the original bias supply wire from its original connecting point in the output stage area, and
3. Isolating the screen grids from the original screen grid supply, and replacing the original screen grid dropping resistor with a new resistor.
Additionally, a terminal strip was added at the top rear of the chassis, with leads running to the cathode terminals of each output tube. With the EFB bias control accessible from the top side of the chassis now (on the EFB board), and the cathode terminals now accessible top side as well, it makes for very easy bias adjustments on the amplifier. The terminal strip and its leads were also accommodated by small cooling holes at the rear of the chassis, so again, no physical alterations were made for the installation of EFB in the 400.
Side Bar: Many folks prefer to install IBAM circuits, which the EFB modification will easily accommodate. Whether such controls are present or not, I always prefer to install a quad of well matched tubes, as this not only helps ensure the best push-pull balance within a given channel, but also ensures the best performance match between channels as well. My 400 does not currently have an IBAM installed, but does employ a tightly matched quad of NOS tubes, making adjustment of the bias very easy now.
With the EFB modification fully installed now, basic tests were run (on full AC power) to see where things stood. Observations include:
1. Power output remains exactly as it was in stock form, with each channel individually producing 25 watts RMS @ 1 kHz by itself, or 22.5 watts RMS each, with both channels driven.
2. Full power 1 Khz THD with both channels driven now produces an average of just .15% THD. This is a very low distortion level, approaching that of some of the very best vacuum tube amplifiers, and is a major improvement over the original design, where both channels were averaging .95% THD with both channels driven.
Side Bar: Much (>50%) of this is due to the EFB screen supply regulator tightly managing the screen voltage now. In the original design, the screen voltage dropped about 55 volts under worst case conditions, destroying the original low distortion operating point of the stage as power was increased. With EFB, the screen voltage still drops slightly, but now, about 1/5 of the original amount -- and most importantly -- it drops in exact relation to any drop in the plate B+ supply, helping to preserve the low distortion operating point. For pentode output stages, effective control of the screen grid is one of the single most important design requirements to maximize performance from the stage.
3. Because the EFB bias and screen supply regulators both provide significant filtering in addition to providing EFB action, residual power supply hum is now extremely low. Measurements were not made regarding this, but it is now very hard to tell if the unit is even turned on through my Cornwalls with the volume at minimum. Subjectively, there is virtually no power supply hum.
4. Original tests indicated that the low distortion point would be achieved with a total quiescent idle current of 22 ma per tube. But those tests were not actual EFB tests, but simulated EFB tests. With the real deal installed, the low distortion point came in at just 21 ma total quiescent current per tube. This is an unbelievably conservative mode of operation for 7591/7868 class tubes. With an actual plate B+ of 425 vdc, and figuring that 20 ma is flowing to the plate (to account for screen current), that equates to a plate dissipation of just 8.5 watts per tube -- which is just under 45% of the rating for the tube. If that doesn't extend tube life, then nothing will!
5. At quiescent conditions, the screen grids are now running at just over 300 vdc. This is nearly a 100 volt drop from what they were running in the stock design, which has taken away all the stress that the stock design placed on them. The EFB screen supply regulator now maintains the new screen/plate voltage relationship regardless of AC power, power output, or B+ level conditions, maintaining the low distortion operating point of the output stage whether each individually, or both channels are driven to any power level up to maximum power output. An additional huge benefit of the new operating conditions is that the screen grids no longer show any color at all, even when grossly over-driven. This too will have a huge effect not only on tube life, but also in maintaining the tubes' original match conditions: Since the screens now run so much cooler, they will not be inclined to distort their shape, which will help preserve either the original match characteristics of a quad or pair, or the that of the individual tube.
6. The new operating conditions in the output stage not only do not require any screen stability resistors to be installed (although they won't hurt if already installed), but also almost certainly will not require the control grid return resistors to be lowered either. Because the tubes now run so cool (in tube degrees that is), the chance of any reverse grid current effects under the new operating conditions is virtually nil. Like the screen stability resistors, lowering the grid return resistor values certainly won't hurt -- although the phase inverter won't like you for doing it. But that will be dealt with in the next installment.
7. After 3 hours of operation, the power transformer was nicely warm to the touch, but hardly hot, and you could easily keep your entire hand on it for as long as you wished. This is out of case of course, but subjectively, it feels notably cooler than with the stock circuit. With a reduction of quiescent current in the output stage of nearly 45 ma, this equates to over 100 ma of current no longer being drawn from the power transformer, considering its voltage doubler configuration, and the charging current required by the doubler caps for the operating current saved.
Pics include:
1. The completed board awaiting installation, glitch free. Green lead group is for the EFB bias supply regulator, red lead group is for the EFB screen supply regulator.
2. Close up detail of the Mosfet mounting. In operation, there is no discernible heat generated by the Mosfet after hours of normal operation, or 1/2 hour of operation at full power output in both channels, ensuring its long life.
3. Detail of the lead groups dropping below the chassis.
4. The completed top side installation. The bias control is easily accessible at the top right of the board.
5. Terminal strip for monitoring output tube current draw.
Next time: Underside shots of the installation, and clean up work: dealing with that pesky phase inverter.
Dave
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